gmerkt
New member
I work on lots of Kenmore uprights, the abundant common machines of 10-15 year old vintage. One of the things I find out of order from time to time concerns the wheels. They are mounted on a common metal axle at the bottom of the main case/housing. The metal axle is held in place by tabs molded into the plastic main case. Sometimes people get too rough with the machine and drop it on a wheel. They won't take a great deal of this before the material that holds the axle in place breaks. The hole becomes over-size. There isn't too much clearance between the wheel and the main case. When the hole gets broken out, it causes interference between the wheel and the case. The wheel is plastic and usually has a rubber tire over it held in place by a groove. When I get one of these missing the tire, it usually means that the machine has been dropped and someone removed the tire from the wheel to recover some of the clearance between it and the main case. So the machine will actually roll again.
To fix this problem requires changing the main case. Usually, I have enough donor machines around for parts to do this. But I get tired of changing everything from one case to the other. Especially the hose. So I decided to come up with a repair to save the broken case.
I considered a number of possibilities but settled on coming up with some kind of bushing to replace the material broken out of the original hole. I pawed through my selection of bronze bushings in the garage, but didn't have what I wanted. The axle measures .25 and the broken out hole sizes in the plastic main case vary. So I thought about using a spent brass cartridge case for making my own bushing. I found that .30 US Carbine cases work well. The hole may only be broken out so far by the limiting factor of the wheel diameter. The .30 US Carbine case measures .35 o.d.; I found a drill bit sized 23/64 (1/4 was a little too large) that worked. I decapped the cartridge case primer and drilled the flash hole and primer pocket out to .25.
Having drilled out the broken hole in the main case to 23/64, next I took some epoxy compounded for plastic and cemented the new "bushing" (cartridge case) into the new hole. I placed the axle through the bushing to get it aligned with the existing hole on the opposite side. After the initial epoxy dried, next I mixed up some bulk epoxy (like they sell for repairing boats, comes in pint cans) and flooded the well area where the new bushing protruded into the inside of the main case. Before applying this bulk epoxy, I roughed up the surface (with a Dremel tool and abrasive bit) of the area in the case where it would make contact to give it a bit of extra "tooth."
Also, check the axle to make sure it's straight. When a machine gets thrown or dropped hard enough to break the case, sometimes the axle also gets bent. A bent axle usually can be easily straightened in a vise.
On this project, I was working on the cases of two machines. The hole was broken out in different sides of each. The machines I was working on happened to be Direct Drive Beltless models, such as the one shown below but this same procedure will work for the very many lower-level, belt-driven models.

To fix this problem requires changing the main case. Usually, I have enough donor machines around for parts to do this. But I get tired of changing everything from one case to the other. Especially the hose. So I decided to come up with a repair to save the broken case.
I considered a number of possibilities but settled on coming up with some kind of bushing to replace the material broken out of the original hole. I pawed through my selection of bronze bushings in the garage, but didn't have what I wanted. The axle measures .25 and the broken out hole sizes in the plastic main case vary. So I thought about using a spent brass cartridge case for making my own bushing. I found that .30 US Carbine cases work well. The hole may only be broken out so far by the limiting factor of the wheel diameter. The .30 US Carbine case measures .35 o.d.; I found a drill bit sized 23/64 (1/4 was a little too large) that worked. I decapped the cartridge case primer and drilled the flash hole and primer pocket out to .25.
Having drilled out the broken hole in the main case to 23/64, next I took some epoxy compounded for plastic and cemented the new "bushing" (cartridge case) into the new hole. I placed the axle through the bushing to get it aligned with the existing hole on the opposite side. After the initial epoxy dried, next I mixed up some bulk epoxy (like they sell for repairing boats, comes in pint cans) and flooded the well area where the new bushing protruded into the inside of the main case. Before applying this bulk epoxy, I roughed up the surface (with a Dremel tool and abrasive bit) of the area in the case where it would make contact to give it a bit of extra "tooth."
Also, check the axle to make sure it's straight. When a machine gets thrown or dropped hard enough to break the case, sometimes the axle also gets bent. A bent axle usually can be easily straightened in a vise.
On this project, I was working on the cases of two machines. The hole was broken out in different sides of each. The machines I was working on happened to be Direct Drive Beltless models, such as the one shown below but this same procedure will work for the very many lower-level, belt-driven models.
